Industrial Utility Efficiency

Industries

The new solution also saves close to 90 percent of the annual maintenance costs. The side channel blowers required intensive repairs and were therefore a source of high costs. MINK MV claw vacuum pumps provide completely dry compression of intake air and thus work without operating fluids such as oil or water. This makes the vacuum pumps virtually maintenance-free. 

Handling Corrugated Cardboard with Optimized Pressure-Regulation of Air-Driven Vacuum Pumps

Using suction cups and air-driven vacuum pumps is a preferable gripping and handling method of corrugated cardboard materials and boxes in carton-machines like case/carton erectors and rotary cartoners. Robot based applications, like palletizing and de-palletizing, are other examples where the best practice technology for gripping and handling is by suction cups and air-driven vacuum pumps.

 

Pneumatech® Biogas Dryers and ConservAir® Flow Controllers

Energy efficiency and sustainability solutions are often associated with more obvious initiatives--such as installing compact fluorescent bulbs—but those solutions fail to dig deeper for the “hidden gems” that can have a much greater impact. For manufacturing and building engineers or anyone else dealing with high potential energy consumption and inrush current demands, compressed air systems are one of the first places to look for significant energy savings and greater sustainability.

Improved Aeration Efficiency through Design and Control

With the recent and future increases of the cost of energy, operating a wastewater treatment plant (WWTP) as efficiently as possible has become one of the most important factors that operators and managers are facing today. The implementation of a properly designed aeration control system has been reported by the United Sates Environmental Protection Agency to reduce aeration energy by 25 to 40 percent.

O₂ Automation: The Future of Bubble Mixing?

We have industrial accounts where we mix chemicals and acids. Our favorite is blending wine and spirits using compressed nitrogen. The old way to blend was to use “air rousing.” This was done by installing rows of perforated pipes in the bottom of the tank and attaching an air pipe to this grid. Since the typical mixing cycle was 45 minutes, copious amounts of air and energy were used.

Adaptive Control for Low Pressure Wastewater Treatment Air Systems

In recent years, there have been many changes in wastewater treatment. Most modern processes control three cycles: DO, NH4, and NO3, and all of the processes require high volumes of air. Undeniably, the low pressure air system uses more electrical power than the rest of the wastewater treatment plant combined. The blower packages in these systems can be equipped with low noise enclosures, fixed speed or variable speed drives, and can include all the instrumentation needed for self-protection.

 

Aeration Energy Offers Opportunities to Save

Aeration systems at wastewater treatment facilities present significant, cost-effective energy savings opportunities. Aeration—the introduction of air into the wastewater stream to support anaerobic bacteria and mixing—is a key function at the majority of wastewater treatment facilities in North America. Aeration accounts for 25-60 percent of total energy consumption at wastewater treatment facilities , and a significant piece of operating budgets sector-wide.

Black & Veatch Provides Guidance to WWTP Design

Blower & Vacuum Best Practices® Magazine interviewed Ms. Julie Gass P.E., Lead Process Mechanical Engineer, from Black & Veatch on trends in the wastewater treatment industry especially pertaining to new technology aeration blowers and energy efficiency.

Furniture Maker Goes with Tri-Lobe Blowers

A large custom leather furniture manufacturer switches from rotary screw vacuum pumps to blowers for CNC router table hold down, and saves big on electricity, maintenance expenses and floor space.

Food Industry Factory Saves $154,000 in Annual Energy Costs

This food industry factory, located in California, was spending \$386,533 annually on energy to operate their compressed air system. This system assessment detailed eleven (11) project areas where yearly energy savings totaling \$154,372 could be found with a investment of \$289,540. A local utility energy incentive, paying 9 cents/kWh, provided the factory with an incentive award of \$159,778. This reduced the investment to \$129,762 and provided a simple ROI of ten months on the project.

Bottler Best Practices in California

Bottling companies and breweries, in California, are benefiting from a three-step system assessment process aimed at reducing the electrical consumption of their compressed air systems. The three-step process reduces compressed air demand in bottling lines by focusing on open blowing and idle equipment, and then improves the specic power (reducing the energy consumption) of the air compressors.

Food

Vacuum and protective gas both reduce the activity of oxygen-dependent microorganisms inside the

Wastewater

When a facility plans for a wastewater treatment plants, they typically design based on population

Containers

Many manufacturing processes are like offensive linemen. When everything is running smoothly,

Auto

The 2023 International Powder and Bulk Solids Conference and Exhibition took place April 25-27,

Plastics

The basic function of vacuum degassing is to remove the vaporized gas and moisture from the

Transit

The IWF 2022 International Woodworking Fair was held August 23-26 at the Georgia World Congress

Pharmaceutical

Ever since it was commissioned in 1974, the Echallens wastewater treatment plant in the Swiss

Auto

The 2023 International Powder and Bulk Solids Conference and Exhibition took place April 25-27,

Energy

Blower & Vacuum Best Practices interviewed Mr. Sid Van der Meer and Mr. Terry Nickel from